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介绍了一种航空发动机加力燃油系统的组成,以及喷口加力调节器和加力燃油分布器等附件的主要功能,对发动机非加力状态加力一区燃油计量活门异常打开故障进行了理论分析,找出了故障原因,并采取有效措施避免再次发生类似故障,为发动机排故提供指导。 相似文献
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针对某型航空发动机在地面应急放油时发生的停车故障,对该型发动机应急放油系统进行了深入的理论分析,并采用5 kHz的采样频率采集数据,进行大量的发动机台架试车和装机试车,通过微观分析,找出该型发动机停车故障的1种特殊原因.在精确分析的基础上,对应急放油系统采取改进设计,并通过试验进行了设计改进后的试车和试飞验证,在应急放油附件管接头通往加力泵接通活门管接头的内部增加φ=1.0 mm的节流嘴,使应急放油接通时主燃油喷嘴前、后压差最低值提高200~700 kPa,并且增加节流嘴后对发动机其他功能和性能无影响,从而可靠地解决了原有应急放油系统的缺陷,有效排除了某型航空发动机在地面应急放油时发生的停车故障. 相似文献
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分析了某型飞机的涡喷七乙发动机加力筒体烧蚀故障情况,对故障机总体及外圈加力总管和加力简体进行了检查,并对故障机进行了台架试车及故障再现试验,确定了故障机加力简体烧蚀烧穿的直接原因是外圈加力总管严重变形,提出了预防故障的措施和建议。 相似文献
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以加力燃油调节器在航空发动机地面台架试车中出现的出口压力波动问题为研究对象,通过理论分析、AMEsim仿真、流体仿真等手段得到了导致压力波动的因素,并据此对该加力燃油调节器进行了优化改进设计。研究表明:通过降低介质流速、改进流道结构、优化压差活门参数匹配特性等措施,可以解决出口压力波动问题。研究成果可为同类燃油调节器的设计、改进和工程排故提供参考。 相似文献
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为获得加力燃油系统数字化仿真与性能验证平台,采用功能划分的方法分析了典型计量装置的功能模块,确定了伺服阀-随动活塞、计量活门-等压差活门是决定计量装置动态特性的主要组成部分,对其进行了数学建模。鉴于获得的数学模型描述系统特性时缺乏相关元件特性参数的设计依据,建立了由计量活门、等压差活门、电液伺服单元等组成计量装置的AMESim模型,计算主要结构参数后仿真分析了其稳态和动态特性。结果表明:基于控制系统构成的加力燃油计量装置功能划分与数学建模可为仿真研究与参数设计提供指导,AMESim可用于动态过程仿真与性能预测。 相似文献
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航空发动机导流叶片角度调节参数变化故障分析 总被引:1,自引:1,他引:0
某型发动机低压压气机进口导流叶片角度α1,其电子调节部分执行机构电磁活门的占空比(Sα),在整个调节过程中是起关键作用的重要参数,但在台架试车过程中曾多台次出现在不同次检查时Sα数值变化的故障。通过对α1主调节系统工作原理的深入分析,确定试车中Sα变化故障是由于燃油调节机构掺混入空气所致,并得到试车验证。本研究对发动机试车中类似故障的排除具有重要的参考意义。 相似文献
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基于飞机油箱模型形状特征油量测量切片步长选择方法研究 总被引:1,自引:0,他引:1
在分析飞机数字式油量测量过程中目前广泛使用的切片法油量测量原理的基础上,针对现有的定步长切片法无法得到准确、可靠的燃油质量特性数据库的缺陷,结合对飞机油箱模型形状特征的分析,提出了基于飞机油箱模型形状特征的油量测量切片步长选择方法。此方法包括切片步长整体和局部选择两个过程,整体选择以实现相邻两切片平面所夹油箱模型体积近似相等为目的来确定切片步长,以体现油箱模型截面整体变化规律;局部选择以设计切片平面与截面突变平面重合或尽可能接近的方式,突出油箱截面的局部变化特征。实验结果表明:该切片步长选择方法较定步长方法能够建立更为合理、可靠的燃油质量特性数据库,从而提高了油量测量精度。 相似文献
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The effect of inlet conditions on the flow and heat transfer in multiple rotating cavity with axial throughflow 总被引:1,自引:0,他引:1
This paper discusses experimental results from two different build configurations of a heated multiple rotating cavity test rig.Measurements of heat transfer from the discs and tangential velocities are presented.The test rig is a 70% full scale version of a high pressure compressor stack of an axial gas turbine engine.Of particular interest are the internal cylindrical cavities formed by adjacent discs and the interaction of these with a central axial throughflow of cooling air.Tests were carried out for a range of non-dimensional parameters representative of high pressure compressor internal air system flows(Re up to 5×106 and Rez up to 2×105).Two different builds have been tested.The most significant difference between these two build configurations is the size of the annular gap between the(non-rotating) drive shaft and the bores of the discs.The heat transfer data were obtained from thermocouple measurements of surface temperature and a conduction solution method.The velocity measurements were made using a two component,LDA system.The heat transfer results from the discs show differences between the two builds.This is attributed to the wider annular gap allowing more of the throughflow to penetrate into the cavity.There are also significant differences between the radial distributions of tangential velocity in the two builds of the test rig.For the narrow annular gap,there is an increase of non-dimensional tangential velocity V/Ωr with radial location to solid body rotation V/Ωr=1.For the wider annular gap,the non-dimensional velocities show a decrease with radial location to solid body rotation. 相似文献
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Abnormal Shape Mould Winding 总被引:1,自引:0,他引:1
Fu Hongya Wang Xianfeng Han Zhenyu Fu Yunzhong 《中国航空学报》2007,20(6):552-558
为解决网格化芯模的缠绕问题,本文提出了复合材料面片缠绕机理;接着详细分析了面片缠绕过程中的芯模凹曲面上纤维滑线和架空现象,应用微分几何曲面理论和空间几何理论,提出判据及其解决方案;最后,针对飞机发动机进气道的缠绕成型,编制缠绕控制程序并进行相应的实验,验证了面片缠绕方法的可行性。 相似文献
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航天器返回地球的气动特性综述 总被引:4,自引:0,他引:4
航天器返回地球的飞行过程中,气动特性是实现将宇宙飞行速度减到落地前速度、保证再入飞行得到有效控制以及再入防热安全可靠的关键因素。针对简单旋成体气动外形、半弹道式再入控制、烧蚀防热类返回航天器,综述了返回地球过程中变化的空气流域特性、航天器周围的气体绕流环境、空气与航天器作用产生的动力学与热效应等。系统地给出了该类航天器的再入气动特性参数与飞行性能的共性规律,包括:气动阻力与再入减速、气动升力与再入轨迹控制、配平攻角与飞行稳定性、气动加热与防热,以及再入过程中不同气动特性航天器、气象条件变化等对再入飞行性能的影响规律。为航天器开展返回飞行过程的跨流域气动性能工程研制提供设计参考。 相似文献
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Research on Auto-detection for Remainder Particles of Aerospace Relay Based on Wavelet Analysis 总被引:2,自引:0,他引:2
GAO Hong-liang ZHANG Hui WANG Shu-juan 《中国航空学报》2007,20(1):75-80
Aerospace relay is one kind of electronic components which is used widely in national defense system and aerospace system. The existence of remainder particles induces the reliability declining, which has become a severe problem in the development of aerospace relay. Traditional particle impact noise detection (PIND) method for remainder detection is ineffective for small particles, due to its low precision and involvement of subjective factors. An auto-detection method for PIND output signals is proposed in this paper, which is based on direct wavelet de-noising (DWD), cross-correlation analysis (CCA) and homo-filtering (HF), the method enhances the affectiv-ity of PIND test about the small particles. In the end, some practical PIND output signals are analysed, and the validity of this new method is proved. 相似文献
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Effects of Mo on the Microstructure and Hydrogen Sorption Properties of Ti-Mo Getters 总被引:1,自引:0,他引:1
ZHOU Hong-guo WEI Xiu-ying MAO Chang-hui XIONG Yu-hua QIN Guang-rong 《中国航空学报》2007,20(2):172-176
The effects of Mo on the microstructure evolution, porosity and hydrogen sorption properties of Ti-Mo getters are investigated in this work. The results show that the addition of Mo prolongs the densification process of Ti-Mo getters and results in a significant amount of sintered pores. With the Mo content increasing, the porosity of getters firstly increases reaching the maximum value as it at- tains about 7.5wt.%, and then drops. At the room temperature, the hydrogen sorption property of getters increases progressively with the Mo content increasing, but the tendency is not very clear before its content lies below 2.5wt.%. When the Mo content achieves about 7.5wt.%, the hydrogen sorption property proves to be the best. The discussion is made about the above mentioned phenomena inclusive of hydrogen sorption properties of getters under different activation conditions (from 500-750 ℃). 相似文献
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YANG Fen ZHANG Xue-jun TIAN Fang WU Xu GAN Fu-xing 《中国航空学报》2007,20(2):181-186
Antimony-doped tin hydroxide colloid precipitates have been synthesized by hydrolysis of SnCl4 and SbCl3 using: (1) an ion-exchange hydrolysis to remove chlorine ions, and (2) isoamyl acetate as an azeotropic solvent to obviate water. The obtained dried powder is of high dispersivity without any need for further grinding. The size and dispersivity of the final particles are investigated with the aid of TG-DTA, BET, XRD and TEM. After having calcined, the antimony-doped tin oxide nanopowder possesses a tetragonal rutile structure with high dispersivity, uniform particles and low hard agglomeration. 相似文献