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某双脉冲发动机燃烧室两相流场数值分析
引用本文:孙娜,娄永春,孙长宏,沈铁华.某双脉冲发动机燃烧室两相流场数值分析[J].固体火箭技术,2012,35(3):335-338.
作者姓名:孙娜  娄永春  孙长宏  沈铁华
作者单位:上海航天动力技术研究所,上海,201109
摘    要:某双脉冲固体火箭发动机试验后出现一脉冲绝热层纵向烧蚀不均匀现象,一脉冲前段绝热层出现“凹坑”.为了解其原因,应用数值计算方法,采用FLUENT计算平台,对此发动机燃烧室内两相流场进行了数值模拟.计算结果表明,由于双脉冲发动机级间通道的存在,使得燃气流在一脉冲燃烧室内出现后台阶流动,气流发生分离再附着过程,气流再附着点附...

关 键 词:双脉冲固体火箭发动机  两相流  燃烧室  数值分析

Numerical analysis of two-phase flow in combustion chamber of dual-pulse motor
SUN Na , LOU Yong-chun , SUN Chang-hong , SHEN Tie-hua.Numerical analysis of two-phase flow in combustion chamber of dual-pulse motor[J].Journal of Solid Rocket Technology,2012,35(3):335-338.
Authors:SUN Na  LOU Yong-chun  SUN Chang-hong  SHEN Tie-hua
Institution:(Shanghai Space Propulsion Technology Research Institute,Shanghai 201109,China)
Abstract:The lengthways erosion of the insulation in the dual-pulse solid rocket motor was uneven after the experimentation,and the pit appeared on the insulation of the forepart of I-pulse-chamber.In order to find out the reason of this phenomenon,the numerical simulation of two-phase flow in the combustion chamber was made with FLUENT.The backward-facing step flow appears in I-pulse-chamber,because of the channel between the I and II chamber of the dual-pulse SRM,which causes the flow separation.From the simulation result,the serious erosion of the insulation in I-pulse-chamber occurs on the place of reattachment and the part of the particles ablation.Therefore,the flow reattachment and the particles ablation are the important causes of the uneven erosion of the insulation in I-pulse-chamber.
Keywords:dual-pulse solid rocket motor  two-phase flow  combustion chamber  numerical simulation
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