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提高二冲程煤油发动机抗爆性措施研究
引用本文:丁昌露,杨海青,陈方超.提高二冲程煤油发动机抗爆性措施研究[J].航空动力学报,2017,32(12):2972-2980.
作者姓名:丁昌露  杨海青  陈方超
作者单位:1.南京航空航天大学 能源与动力学院,南京 210016
基金项目:江苏省普通高校研究生科研创新计划(KYLX15_0262)
摘    要:为解决某二冲程航空活塞发动机采用航空煤油后爆震极限功率严重下降的问题,进行了一维发动机性能仿真分析,提出了提高发动机爆震极限功率的技术措施。在发动机额定工况下,油耗率和排气温度不发生恶化的前提下,添加抗爆添加剂、降低压缩比和推迟点火提前角以抑制采用煤油后的发动机爆震倾向,扩大缸径和降低空燃比以助于恢复发动机的爆震极限功率。结果表明:经过优化,发动机输出功率可达到原型机的96%,油耗率增加了19%,排气温度升高了57K。研究结果可为二冲程煤油发动机的性能优化和提高工作的可靠性提供依据。 

关 键 词:二冲程发动机    低辛烷值燃料    抗爆性    一维性能仿真    性能优化
收稿时间:2016/7/8 0:00:00

Study on anti knock quality strategies of two stroke kerosene engine
Abstract:An one dimensional performance simulation was made to solve the problem that the knock limited power of a 2 stroke aviation engine decreases due to the use of aviation kerosene. Several technical measures were proposed to boost the knock limited power of engine. Under the rated condition that specific fuel consumption and exhaust temperature did not deteriorate, adding anti knock additive, decreasing compression ratio and retarding ignition timing mitigated the knock tendency after using kerosene as the fuel instead of gasoline. Enlarging cylinder diameter and decreasing the Air fuel ratio were beneficial to the recovery of knock limited power of engine. Result showed that,after optimization, the engine regained 96% of original output power. The specific fuel consumption increased by 19% and exhaust temperature increased by 57K. The research results provide the basis for performance optimization and work reliability of two stroke kerosene engine. 
Keywords:two stroke engine  low octane fuel  anti knock quality  one dimensional performance simulation  performance optimization
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