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诱导轮与叶轮组合式航空燃油离心泵轴向力间隙补偿
引用本文:李嘉,李华聪,王淑红,徐轩.诱导轮与叶轮组合式航空燃油离心泵轴向力间隙补偿[J].航空动力学报,2016,31(11):2765-2772.
作者姓名:李嘉  李华聪  王淑红  徐轩
作者单位:1. 西北工业大学动力与能源学院,西安,710072;2. 中国航空发动机集团有限公司西安航空动力控制科技有限公司,西安,700077
摘    要:以诱导轮与叶轮组合式航空燃油离心泵为研究对象,开展了轴向力出口间隙补偿优化研究.进行了轴向力的数值模拟,并将仿真结果与理论计算进行对比,对比表明两种方法计算的轴向力结果变化趋势一致,误差不大于4%,且设计流量工况下误差最小,进而验证了基于Pumplinx环境下该型离心泵轴向力数值仿真的正确性.通过改变出口间隙宽度分析离心泵的轴向力变化,仿真结果表明:扩大出口间隙至0.2mm时,增大了轴向力,且影响了泵的增压能力;而减小出口间隙至0.1mm和0.13mm时实现了轴向力的补偿,且出口间隙为0.1mm时性能最优.最后对出口间隙为0.1mm时的轴向力性能进行了分析,分析表明:该条件下不同截面的压力分布正常稳定,且设计点的轴向力为3620N,从而实现了诱导轮与叶轮组合式离心泵的轴向力间隙补偿.

关 键 词:航空燃油离心泵  诱导轮与叶轮  组合式  轴向力  出口间隙补偿
收稿时间:2015/2/13 0:00:00

Outlet clearance optimization on axial-force of inducer and impeller combination aero fuel centrifugal pump
LI Ji,LI Hua-cong,WANG Shu-hong and XU Xuan.Outlet clearance optimization on axial-force of inducer and impeller combination aero fuel centrifugal pump[J].Journal of Aerospace Power,2016,31(11):2765-2772.
Authors:LI Ji  LI Hua-cong  WANG Shu-hong and XU Xuan
Institution:School of Power and Energy, Northwestern Polytechnical University, Xi''an 710072,School of Power and Energy, Northwestern Polytechnical University, Xi''an 710072,Xi''an Aero-Engine Controls Technology Company Limited, Aero Engine(Group) Corporation of China, Xi''an 700077, China and Xi''an Aero-Engine Controls Technology Company Limited, Aero Engine(Group) Corporation of China, Xi''an 700077, China
Abstract:As the research object of inducer and impeller combination aero fuel centrifugal pumps, the outlet clearance optimization on axial-force of the pump was carried out. Through comparing the axial-force simulation data with theoretical calculation data, the axial-force trends of the two methods were identified similar and the simulation''s accuracy was verified by Pumplinx because of the error less than 4%. Then the outlet clearance''s influence on axial-force was analyzed. Simulation results show that expanding the clearance to 0.2mm increases the axial-force value, and reduces the pressure charging; but reducing the clearance to 0.1mm and 0.13mm can make optimizations of the axial-force, and the clearance of 0.1mm is the best. The axial-force performance of the model with clearance of 0.1mm was analyzed finally, showing that this model''s inner performance of different sections is normal and steady; the axial-force value at design point is 3620N, so reducing the outlet clearance to 0.1mm can make a high optimization about axial-force of the inducer and impeller combination centrifugal pump.
Keywords:aero fuel centrifugal pump  inducer and impeller  combination  axial-force  outlet clearances optimization
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