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171.
针对船用大功率柴油机瞬态性能提升的需求,开展了增压中冷船用大功率柴油机瞬态工况动态响应及燃烧特性实验研究。研究表明,涡轮增压器惯性导致的进气滞后是柴油机瞬态工况下性能恶化的主要原因;突加载工况下,进气量响应滞后供油量响应4~5个工作循环,且进气量响应速度随初始负荷增加而增加,指示平均有效压力(Indicated Mean Effective Pressure,IMEP)等燃烧特征参数加载过程中响应速度较快,波动较小;缸内燃烧过程恶化,燃烧重心和燃烧终点较同负荷下稳态工况值均推迟。 相似文献
172.
Flight risk prediction is significant in improving the flight crew’s situational awareness because it allows them to adopt appropriate operation strategies to prevent risk expansion caused by abnormal conditions, especially aircraft icing conditions. The flight risk space representing the nonlinear mapping relations between risk degree and the three-dimensional commanded vector(commanded airspeed, commanded bank angle, and commanded vertical velocity) is developed to provide the crew with practi... 相似文献
173.
《中国航空学报》2023,36(3):16-29
Geometric and working condition uncertainties are inevitable in a compressor, deviating the compressor performance from the design value. It’s necessary to explore the influence of geometric uncertainty on performance deviation under different working conditions. In this paper, the geometric uncertainty influences at near stall, peak efficiency, and near choke conditions under design speed and low speed are investigated. Firstly, manufacturing geometric uncertainties are analyzed. Next, correlation models between geometry and performance under different working conditions are constructed based on a neural network. Then the Shapley additive explanations (SHAP) method is introduced to explain the output of the neural network. Results show that under real manufacturing uncertainty, the efficiency deviation range is small under the near stall and peak efficiency conditions. However, under the near choke conditions, efficiency is highly sensitive to flow capacity changes caused by geometric uncertainty, leading to a significant increase in the efficiency deviation amplitude, up to a magnitude of ?3.6%. Moreover, the tip leading-edge radius and tip thickness are two main factors affecting efficiency deviation. Therefore, to reduce efficiency uncertainty, a compressor should be avoided working near the choke condition, and the tolerances of the tip leading-edge radius and tip thickness should be strictly controlled. 相似文献
174.