排序方式: 共有106条查询结果,搜索用时 31 毫秒
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通过试验、分析、比较,提出了高温、高稳定性压电元件的研制要求,并确认了铋钛系列晶体是制作压电加速度传感器较理想的材料. 相似文献
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《中国航空学报》2021,34(4):526-539
This paper proposes a Linkage Learning Genetic Algorithm (LLGA) based on the messy Genetic Algorithm (mGA) to optimize the Min-Max fuel controller performance in Gas Turbine Engine (GTE). For this purpose, a GTE fuel controller Simulink model based on the Min-Max selection strategy is firstly built. Then, the objective function that considers both performance indices (response time and fuel consumption) and penalty items (fluctuation, tracking error, overspeed and acceleration/deceleration) is established to quantify the controller performance. Next, the task to optimize the fuel controller is converted to find the optimization gains combination that could minimize the objective function while satisfying constraints and limitations. In order to reduce the optimization time and to avoid trapping in the local optimums, two kinds of building block detection methods including lower fitness value method and bigger fitness value change method are proposed to determine the most important bits which have more contribution on fitness value of the chromosomes. Then the procedures to apply LLGA in controller gains tuning are specified stepwise and the optimization results in runway condition are depicted subsequently. Finally, the comparison is made between the LLGA and the simple GA in GTE controller optimization to confirm the effectiveness of the proposed approach. The results show that the LLGA method can get better solution than simple GA within the same iterations or optimization time. The extension applications of the LLGA method in other flight conditions and the complete flight mission simulation will be carried out in part II. 相似文献
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为了研究后挡板结构对刷式密封泄漏特性的影响,模拟航空发动机静态和动态工况,对三种不同后挡板结构的刷式密封泄漏特性进行实验研究。实验结果表明:相比于标准型刷式密封,后挡板结构中设计环形平衡腔能有效缓解刷式密封刷丝滞后效应,但间隙值过大将导致刷式密封性能下降;刷式密封实验件b(有环形平衡腔,与刷丝束之间的间隙为0.2mm)的泄漏参数Φ2保持在7 g﹒K1/2﹒mm/(N﹒s)以内,表现出优异的密封性能,这说明合适的环形平衡腔间隙值设计,能有效缓解刷式密封刷丝滞后现象。根据实验结果,环形平衡腔的间隙设计值应不大于0.4mm。 相似文献
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为了验证多级轴流压气机出口级性能,开展四级重复级低速模拟气动设计,并坚持以二维设计为主,三维数值验证为辅。利用相同的设计系统,建立了高低速压气机之间相似的二维流场和叶表无量速度分布。随后,低速与高速压气机三维数值计算结果对比表明,压升系数特性吻合,流场相似,且叶表无量纲速度由设计点到失速点保持一致的变化趋势,进一步验证了二维设计的可行性;利用相同的系统设计高、低速压气机,有利于形成高速-低速-高速的良性循环,有利于完善基于通流程序的设计体系,积累设计经验。 相似文献
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满足二次稳定及干扰抑制性能指标的航空发动机H∞控制器设计 总被引:1,自引:1,他引:0
对于一类状态及输出矩阵存在结构参数摄动的对象,本文提出了闭环系统满足二次稳定性及干扰抑制性能的动态输出反馈控制器的理论设计方法,随后进行的仿真结果表明,所设计的控制器满足要求。 相似文献
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《中国航空学报》2021,34(2):28-53
Because of several advantages, such as no tool wear, independence on the mechanical properties of the material, and high machining efficiency, electrochemical machining (ECM) has become a viable method for machining components in numerous industrial applications, particularly in the manufacture of typical aero-engine components with complex structures fabricated from materials that are difficult to cut. This paper highlights the current developments, new trends, and technological advances of key factors of ECM, such as electrochemical dissolution characteristics of novel difficult to cut materials which are often used in aero-engine, numerical simulation of electrochemical process, design for the complex profile and structure of cathode tool, flow field simulation and design for uniform electrolyte flow, and innovation of electrochemical machining or hybrid methods which reflect the state of the art in academic and industrial research on electrochemical machining in aero-engine manufacturing. 相似文献