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《中国航空学报》2023,36(2):1-16
In this study, the influence of inter-stage bleeding on the compressor performance and inter-stage flow field of a multistage axial compressor is investigated by both experimental and numerical methods. The experiment is conducted on a four-stage low-speed axial compressor, and a specific computational model is built to simulate the experiment environment accurately. To illuminate the fluid mechanisms of bleeding effect in detail, both the experiment and the simulation are carried out twice, i.e., in the first time, the mass flow rate upstream the bleed location is constant under different bleed rate conditions; while in the second time, the mass flow rate downstream the bleed location is constant under different bleed rate conditions. The results demonstrate that inter-stage bleeding has little influence on upstream compressor characteristics, and affects the upstream flow field only in the rear half of the stator. The bleed effect on the downstream flow field is embodied in the variation of an incoming flow profile, an increase as the compressor inlet flow coefficient decreases. Therefore, such an effect is only significant on compressor characteristics at small flow coefficient conditions. In multistage compressors, the variation of compressor characteristics and flow field caused by inter-stage bleeding is the comprehensive result of the bleeding and the variation of the upstream working condition. In addition, the comparison between numerical and experimental results shows that the flow moves towards top half of span through the downstream rotor passage in the numerical simulation, whereas the trend of flow field variation with different bleed rates at the outlet of the downstream rotor and stator is the same with that at the inlet of the downstream rotor in the experiment, which means that the numerical method has overestimated the radial mixing intensity of the flow. 相似文献
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玉米空间飞行处理细胞超微结构变异的研究 总被引:1,自引:0,他引:1
玉米干种子搭载于返回式卫星上,经离海平面176km至354km的空间条件处理,发现处理后的玉米叶片超微结构发生各种变异。主要变异包括:细胞质壁分离,液泡增大,细胞壁加厚、扭曲,胞间连丝增多,出现叶绿体基粒盘和基质类囊体的变异,细胞核和叶绿体变形,内质网的数量增多、体积增大,以及其它细胞内膜系统与其它超微结构的变化。 相似文献
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The aerodynamic interaction effect of rotorwake on fuselage isan importantproblem in designof helicopter. It affects flight performance,equi-librium,control stabilization and vibrational level.The developing trend of modern helicopter is thatthe size is towards more compact and the load ofrotor disk is towards heavier. The load of rotordisk is about 2 0 kg/ m2 in the 5 0 s,but for modernhelicopter it is up to about 5 0 kg/ m2 . Therefore,the strong rotor wake impacting the closerfuselageand t… 相似文献
769.
有声腔燃烧室的声学特性实验 总被引:3,自引:2,他引:1
为了掌握声腔对燃烧室声学特性的影响规律,采用冷态实验方法,研究了带有轴向直圆孔声腔的模拟燃烧室的声学特性,其中声腔长度、开口面积比(声腔横截面积除以燃烧室横截面积)和个数均可调节.研究结果表明:燃烧室固有频率随声腔长度的增加而逐渐减小;声腔存在最佳深度,能够抑制一阶切向振型,该最佳深度不受声腔开口面积比影响,略小于1/4一阶切向波长;对抑制一阶切向振型而言,声腔存在最佳开口面积比,在本研究中约为0.17;声腔的分布对燃烧室的声学特性影响较大,相同开口面积比下,声腔个数越多,声波衰减越快. 相似文献
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