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51.
韩丹 《中国民航学院学报》2011,(4):31-34
在现有的地空通信遥控系统中,语音交换和控制系统即内话系统所采用的比选技术很难保证输出语音信号的质量。提出结合比选技术和改进的谱减法来增强地空通信语音质量,并给出了实现方案。最后利用DSP实现了内话系统语音增强的原型实验系统,实验结果表明系统达到了语音比选以及增强的目的。 相似文献
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基于体积力方法将压气机叶片对气流的作用力和做功简化为源项,对环形无叶片通道求解带源项的Navier-Stokes(N-S)方程,实现了压气机全通道流场的计算,通过在转子上游机匣施加射流建立了轴流压气机叶尖射流扩稳数值模型.模型中的源项根据叶片排进口气流参数进行变化,通过判断施加的人工扰动变化确定压气机失稳边界.采用该模型对某跨声速单级压气机在有、无射流下的性能和稳定性进行了计算分析,无射流下计算的该压气机性能和稳定边界与试验结果都能较好地一致,其中稳定边界流量仅相差0.7%;有射流下射流对压气机具有明显的扩稳效果,将计算结果与国外公开文献的结果进行了对比,验证了模型的可靠性. 相似文献
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An experimental study was conducted to investigate the evolutions of unsteady vortex structures downstream a lobed mixer/nozzle.Anovel dual-plane stereoscopic PIVsystem was used to measure all 3-components of vorticity distributions to revealed both the large-scale streamwise vortices produced by the lobed mixer/nozzle and the Kelvin-Helmholtz vortex structures generated due to the Kelvin-Helmholtz instabilities simultaneously and quantitatively for the first time.The instantaneous and the ensemble-averaged vorticity distributions displayed quite different aspects about the evolutions of the unsteady vortex structures.While the ensemble-averaged vorticity distributions indicated the overall effect of the special geometry of the lobed nozzle/mixer on the enhanced mixing process,the instantaneous vorticity distributions elucidated many details about how the enhanced mixing process was conducted.In addition to quantitatively confirming conjectures of previous studies,further insight about the formation,evolution and interaction characteristics of the unsteady vortex structures downstream of the lobed mixer/nozzle were also uncovered quantitatively in the present study. 相似文献
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超临界压力下航空煤油水平管内对流换热特性数值研究 总被引:1,自引:4,他引:1
采用RNG(renormalization group)k-ε湍流模型和近壁区的Wolfstein一方程模型对超临界压力下大庆RP-3航空煤油在水平圆管内的流动和换热特性进行了数值研究.超临界压力下,由于航空煤油在拟临界点附近热物性的剧烈变化,浮升力将引起显著的二次流动.二次流动使得水平圆管的下表面湍流强度和对流换热增强,而上表面的湍流强度和对流换热减弱.最后分析了两种水平管内对流换热受浮升力影响判别标准在超临界流体中的适用性. 相似文献
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LI Qiang FAN Wei YAN Chuan-jun HU Cheng-qi YE Bin 《中国航空学报》2007,20(1):9-14
The PDRE test model used in these experiments utilized kerosene as the fuel, oxygen as oxidizer, and nitrogen as purge gas. The solenoid valves were employed to control intermittent supplies of kerosene, oxygen and purge gas. PDRE test model was 50 mm in inner diameter by 1.2 m long. The DDT (deflagration to detonation transition) enhancement device Shchelkin spiral was used in the test model. The effects of detonation frequency on its time-averaged thrust and specific impulse were experimentally investigated. The obtained results showes that the time-averaged thrust of PDRE test model was approximately proportional to the detonation frequency. For the detonation frequency 20 Hz, the time-averaged thrust was around 107 N, and the specific impulse was around 125 s. The nozzle experiments were conducted using PDRE test model with three traditional nozzles. The experimental results obtained demonstrated that all of those nozzles could augment the thrust and specific impulse. Among those three nozzles, the convergent nozzle had the largest increased augmentation, which was approximately 18%, under the specific condition of the experiment. 相似文献