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1.
根据襟翼电气操纵系统的通电故障,叙述了襟翼电气操纵系统功能、故障分析及线路改进过程。通过对机上线路的插头进行分解,进行导通和绝缘检测,排除了机上线路故障;通过对设计线路进行分析,发现在襟翼电气操纵系统与起落架收放操纵及信号系统的交联线路存在回流现象,致使在起落架收放操纵及信号系统通电检查时,襟翼系统不供电的情况下,电流从起落架信号断路器经过起落架信号盒,到襟翼系统的襟翼控制盒、襟翼电磁阀形成回路,导致襟翼在不给电的情况下被放下,设计原理存在严重的缺陷。提出了改进方案。和设计协商确认后,对襟翼电气操纵系统的原理、馈电图做了相应更改,对襟翼电气操纵系统与起落架收放操纵及信号系统进行了功能验证。试验证明:在线路改进后,襟翼电气操纵系统与起落架收放操纵及信号系统功能完好,而且故障得以排除,消除了重大的质量隐患。  相似文献   

2.
针对舰载机电气线路互联系统的腐蚀问题,描述了系统典型部位发生的各类腐蚀现象,分析了腐蚀产生的原因,从设计、制造和维护角度给出了相应的解决措施。该措施经过试验验证,可以解决舰载机电气线路互联系统的腐蚀问题,解决措施具有一定的可行性和实用性。  相似文献   

3.
对民用飞机燃油箱常见的电火花和电弧、细丝加热、摩擦火花和热表面点燃四种点火源进行了介绍,分析了与电缆敷设相关的点火源,总结了可能降低燃油箱安全性的燃油泵布线、燃油量指示系统布线和电气馈电线布线的设计特征,提出了燃油箱布线的基本原则。分别从线路敷设、线路隔离、瞬态抑制装置的使用等方面提出了最小化点火源的可接受布线设计方法,为飞机燃油箱的布线设计和安全性分析提供了指导。  相似文献   

4.
曹涛 《航空工程进展》2020,11(1):140-146
航空电气电弧、短路可能会导致难以挽回的损失,研究航空电气电弧、短路的危害及其保护措施具有 重要意义。通过试验室搭建民用飞机典型的115V/400Hz三相交流电气线路,选取金属导体作为多余物,采 用试验法对飞机电气电弧、短路故障现象进行研究,验证和分析传统热断路器的工作特性,确认电气电弧、短路 故障对电气线路和设备产生的危害程度;同时,分析三种更好的电气电弧、短路保护方法。结果表明:传统热断 路器仅对短路故障具有保护作用,对电气电弧不能产生保护作用;三种新的保护方法电弧检测和保护时间过 长,电弧已对导线和设备产品造成不可恢复的损坏。  相似文献   

5.
我国是世界上火灾发生率较高的国家之一,仅1986年我国火灾次数达38764次,直接经济损失达3.24亿元。在不同的火灾起因中,电气火灾占有较大的比例约15%。 电气火灾原因很多,本文仅对电气线路火灾的某些起因作一些分析。 起火的三个条件是:氧气、可燃物质和火源。电气线路起火也不例外。氧气是无处不有的,而线路附近的纸、棉、油类等物质和电线本身的某些绝缘材料等都是可燃物质。如果电线本身不正常,像连接松动、过载、短路等所产生的电火花,电弧,高温等均形成火源。  相似文献   

6.
为了全面提升军用飞机线束及线束敷设设计质量,从设计源头根本性改善外场线路问题,从系统设计的角度出发,开展了EWIS (电气线路互联系统)设计质量控制的新流程、新方法和新技术的研究和应用。根据设计质量问题和改进需求分析结果,提出了基于PDCA (质量环)的质量控制方法,并将其应用到实践中,完善了EWIS技术文件体系,形成了EWIS精细化设计及检查验证流程,提高了设计要求的提出、实现、验证和持续完善能力,在此基础上优化了对重量特性的控制过程,极大提高了设计质量和效率,对提升飞机EWIS设计质量具有参考意义。  相似文献   

7.
文中研究如何建立飞机电气线路互联系统基础数据库,并进行数据库的管理;研究如何更新基础数据,完成数据统一;建立线束设计统一数据源管理模型,生成用于飞机线束设计的简单有效的基础数据库,使用工具从设计数据中提取来自原始数据的项目清单,并创建比对程序,自动识别差异,用以及时跟踪变更带来的影响。  相似文献   

8.
随着适航新规章的发布,电气线路互联系统(EWIS)在整个民机设计体系中愈发得到重视。国外在EWIS设计方面已形成了非常专业化的体系,通过四个典型实例介绍了国外在EWIS设计中的先进理念,并探讨了对国内EWIS设计的借鉴意义并提出了相关建议。这些典型实例包括:EWIS适航认证、EWIS部件可靠性分析、EWIS安装设计标准制定、EWIS总体布局设计。  相似文献   

9.
在民用飞机电气线路互联系统(EWIS)设计中,通过物理隔离防止电弧和电磁干扰(EMI)是适航审定的重要内容。以隔离距离为研究对象,基于电磁仿真软件CST,构建多种模型,对不同类型线缆间、不同电信号线路进行了仿真,证明了物理隔离不但是防止电弧产生的有效方式,而且能够极大地降低电磁干扰,同时使用屏蔽线缆和多芯扭绞等防护方法,也是降低电磁干扰的有效措施。  相似文献   

10.
针对军用飞机电气线路互联系统(Electrical Wiring Interconnection System,EWIS)的设计特点和现状,明确了EWIS功能定位。在分析军事需求工程(Military Requirement Engineering,MRE)体系框架、过程和方法基础上,以海军飞机EWIS需求开发为例,设计了基于MRE的EWIS需求开发过程和统一需求描述模型,构建了需求体系框架,提出了基于数据的需求管理过程,为军用飞机EWIS设计提供参考依据。  相似文献   

11.
This paper discusses experimental results from two different build configurations of a heated multiple rotating cavity test rig.Measurements of heat transfer from the discs and tangential velocities are presented.The test rig is a 70% full scale version of a high pressure compressor stack of an axial gas turbine engine.Of particular interest are the internal cylindrical cavities formed by adjacent discs and the interaction of these with a central axial throughflow of cooling air.Tests were carried out for a range of non-dimensional parameters representative of high pressure compressor internal air system flows(Re up to 5×106 and Rez up to 2×105).Two different builds have been tested.The most significant difference between these two build configurations is the size of the annular gap between the(non-rotating) drive shaft and the bores of the discs.The heat transfer data were obtained from thermocouple measurements of surface temperature and a conduction solution method.The velocity measurements were made using a two component,LDA system.The heat transfer results from the discs show differences between the two builds.This is attributed to the wider annular gap allowing more of the throughflow to penetrate into the cavity.There are also significant differences between the radial distributions of tangential velocity in the two builds of the test rig.For the narrow annular gap,there is an increase of non-dimensional tangential velocity V/Ωr with radial location to solid body rotation V/Ωr=1.For the wider annular gap,the non-dimensional velocities show a decrease with radial location to solid body rotation.   相似文献   

12.
Aerospace relay is one kind of electronic components which is used widely in national defense system and aerospace system. The existence of remainder particles induces the reliability declining, which has become a severe problem in the development of aerospace relay. Traditional particle impact noise detection (PIND) method for remainder detection is ineffective for small particles, due to its low precision and involvement of subjective factors. An auto-detection method for PIND output signals is proposed in this paper, which is based on direct wavelet de-noising (DWD), cross-correlation analysis (CCA) and homo-filtering (HF), the method enhances the affectiv-ity of PIND test about the small particles. In the end, some practical PIND output signals are analysed, and the validity of this new method is proved.  相似文献   

13.
14.
Antimony-doped tin hydroxide colloid precipitates have been synthesized by hydrolysis of SnCl4 and SbCl3 using: (1) an ion-exchange hydrolysis to remove chlorine ions, and (2) isoamyl acetate as an azeotropic solvent to obviate water. The obtained dried powder is of high dispersivity without any need for further grinding. The size and dispersivity of the final particles are investigated with the aid of TG-DTA, BET, XRD and TEM. After having calcined, the antimony-doped tin oxide nanopowder possesses a tetragonal rutile structure with high dispersivity, uniform particles and low hard agglomeration.  相似文献   

15.
The effects of Mo on the microstructure evolution, porosity and hydrogen sorption properties of Ti-Mo getters are investigated in this work. The results show that the addition of Mo prolongs the densification process of Ti-Mo getters and results in a significant amount of sintered pores. With the Mo content increasing, the porosity of getters firstly increases reaching the maximum value as it at- tains about 7.5wt.%, and then drops. At the room temperature, the hydrogen sorption property of getters increases progressively with the Mo content increasing, but the tendency is not very clear before its content lies below 2.5wt.%. When the Mo content achieves about 7.5wt.%, the hydrogen sorption property proves to be the best. The discussion is made about the above mentioned phenomena inclusive of hydrogen sorption properties of getters under different activation conditions (from 500-750 ℃).  相似文献   

16.
超声速燃烧数值模拟中的湍流与化学反应相互作用模型   总被引:1,自引:0,他引:1  
杨越  游加平  孙明波 《航空学报》2015,36(1):261-273
高精度数值模拟有助于理解超声速湍流燃烧中湍流与化学反应的相互作用,可为发动机燃烧室等工程应用设计提供可靠的预测模型。除直接数值模拟外,目前在湍流燃烧应用中使用的大涡模拟和雷诺平均Navier-Stokes模拟均需要借助模型模化发生在湍流小尺度上的流动与化学反应过程对湍流大尺度运动的影响。现有的湍流与化学反应相互作用模型大致可分为:火焰面类模型和概率密度函数类模型,2类模型在不同的应用中各自具有优势和局限性。此外,现有模型大都基于低马赫数燃烧,而超声速燃烧中通常会伴随快速混合、局部熄火和再着火以及激波等复杂过程,这为发展其中的湍流与化学反应相互作用模型提出了更多的挑战。  相似文献   

17.
适于低轨卫星IP网络的单核共享树组播算法(英文)   总被引:1,自引:0,他引:1  
为了解决低轨卫星IP网络中现有典型源组播算法的信道资源浪费问题,本文提出了一套单核共享树组播算法,即核心群合并共享树(CCST)和加权核心群合并共享树(w-CCST)算法。CCST 算法包括动态近似中心(DAC)选核方法和核心群合并组播路径构建方法。DAC方法专为周期、规律运动的低轨卫星网络提出,不需要复杂的星上计算。在核心群合并方法中,以核节点作为初始核心群,通过核心群和剩余组成员的最短路径方法逐步扩展直至整棵组播树构建完成,从而使得组播树的树代价最小,大大提高了网络的带宽利用率和组播传输效率。w-CCST 算法中所提出的加权因子可以调整树代价和端到端传播时延之间的折衷程度,因此,可以通过调整加权因子来适度增大树代价、降低端到端传播时延以支持某些端到端时延要求苛刻的实时组播业务。最后,与低轨卫星 IP 网络中典型算法进行了性能比较,仿真结果说明,CCST 算法的平均树代价比其它算法显著降低,w-CCST 算法的平均端到端传播时延小于 CCST 算法。  相似文献   

18.
Jet Vectoring Control Using a Novel Synthetic Jet Actuator   总被引:3,自引:1,他引:2  
A primary air jet vectoring control system with a novel synthetic jet actuator (SJA) is presented and simulated numerically. The results show that, in comparison with an existing traditional synthetic jet actuator, which is able to perform the duty of either “push” or “pull”, one novel synthetic jet actuator can fulfill both “push” and “pull” functions to vector the primary jet by shifting a slide block inside it. Therefore, because the new actuator possesses greater efficiency, it has potentiality to replace the existing one in various appli- cations, such as thrust vectoring and the reduction of thermal signature. Moreover, as the novel actuator can fulfill those functions that the existing one can not, it may well be expected to popularize it into more flow control systems.  相似文献   

19.
The slewing motion control of a truss arm driven by a V-gimbaled control-moment-gyro (CMG) is a nonlinear control problem. The V-gimbaled CMG consists of a pair of gyros that must precess synchronously. The moment of inertia of the system, the angular momentum of the gyros and the external disturbances are not exactly known. With the help of feedback linearization and recursive Lyapunov design method, an adaptive nonlinear controller is designed to deal with the unknown items. Performance of the proposed controller is verified by simulation.  相似文献   

20.
A new time-accurate marching scheme for unsteady flow calculations is proposed in the present work. This method is the combination of classical Successive Over-Relaxation (SOR) iteration method and Jacobian matrix diagonally dominant splitting method of LUSGS. One advantage of this algorithm is the second-order accuracy because of no factorization error. Another advantage is the low computational cost because the Jacobian matrices and fluxes are only calculated once in each physical time step. And, the SOR algorithm has better convergence property than Gauss-Seidel. To investigate its accuracy and convergency, several unsteady flow computa- tional tests are carried out by using the proposed SOR algorithm. Roe’s FDS scheme is used to discritize the inviscid flux terms. Un- steady computational results of SOR are compared with the experiment results and those of Gauss-Seidel. Results reveal that the numerical results agree well with the experimental data and the second-order accuracy can be obtained as the Gauss-Seidel for unsteady flow computations. The impact of SOR factor is investigated for unsteady computations by using different SOR factors in this algorithm to simulate each computational test. Different numbers of inner iterations are needed to converge to the same criterion for different SOR factors and optimal choice of SOR factor can improve the computational efficiency greatly.  相似文献   

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