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冲压发动机燃烧室内低频燃烧不稳定试验
引用本文:谭建国,潘余,王振国.冲压发动机燃烧室内低频燃烧不稳定试验[J].推进技术,2011,32(2):188-190.
作者姓名:谭建国  潘余  王振国
作者单位:国防科技大学,航天与材料工程学院,湖南,长沙,410073
摘    要:在高空亚燃冲压发动机研究中,燃烧不稳定是一个突出问题.为解决30km,Ma =4亚燃冲压发动机直连式试验中所出现的低频燃烧不稳定问题,分析了燃烧室的声学特性,得出了燃烧不稳定的主要特征是燃烧放热与一阶纵向声振模态相藕合.采取在燃烧室内增加后向台阶形成凹腔的方法,成功得到了较为稳定的燃烧.

关 键 词:亚燃冲压发动机  燃烧不稳定  低压  声振
收稿时间:2009/10/20 0:00:00
修稿时间:2010/9/20 0:00:00

Experimental research on low-frequency instability in ramjet combustor
TAN Jian-guo,PAN Yu and WANG Zhen-guo.Experimental research on low-frequency instability in ramjet combustor[J].Journal of Propulsion Technology,2011,32(2):188-190.
Authors:TAN Jian-guo  PAN Yu and WANG Zhen-guo
Institution:TAN Jian-guo,PAN Yu,WANG Zhen-guo(lnst.of Aerospace and Material Engineering,National Univ.of Defence Technology,Changsha 410073,China)
Abstract:Combustion instability is one of the most crucial problems for developing high-altitude ramjet.To solve combustion instability problem occurred in a direct-connected experiments of a 30km,Ma=4 ramjet,acoustic characteristics are analyzed.Results show that the main character of combustion instability is due to the coupling of heat release and longitudinal acoustic oscillation.Then relative stable combustion is achieved in cavity-type combustor by adding backward step.
Keywords:Ramjet  Combustion instability  Low pressure  Acoustic oscillation  
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