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低泄漏高寿命刷式封严的实验研究
引用本文:郭霖,康宁.低泄漏高寿命刷式封严的实验研究[J].航空动力学报,2003,18(4):485-487.
作者姓名:郭霖  康宁
作者单位:北京航空航天大学能源与动力工程学院,北京100083
基金项目:航空基金资助项目(00C51084)
摘    要:以相似理论为依据,通过空气动力学的实验方法探索新型低泄漏高寿命3层片式刷式封严结构。以空气泄漏量作为评价指标,确定新型刷式封严结构的密封性并对其进行改进。实验结果表明:改进的3层片状刷式封严结构的密封泄漏特性优于简单的片状刷封结构;随着3层片状刷封进出口压差的增大,泄漏量也随之增大。 

关 键 词:航空、航天推进系统    密封    密封漏泄    空气动力学实验
文章编号:1000-8055(2003)04-0485-03
收稿时间:2002/10/9 0:00:00
修稿时间:2002年10月9日

Experimental Study of Low Leakage and High Endurance Brush Seals
Institution:Beijing University of Aeronautics and Astronautics,Beijing100083,China
Abstract:On the basis of the similarity theory,a new style of brush seals with low leakage and high endurance was studied experimentally in this paper.The brush seal structure was evaluated according to the measured experimental results.The results showed that:the leakage of the new brush seals was smaller than that of the old brush seals;the leakage difference between the two brush seals became larger with the increase of the pressure difference.
Keywords:aerospace propulsion system  sealing  seal leakage  aerodynamic experiment
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