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某型航空活塞发动机进排气系统优化分析
引用本文:徐斌,刘波,杨世春,姬芬竹.某型航空活塞发动机进排气系统优化分析[J].航空动力学报,2014,29(3):624-630.
作者姓名:徐斌  刘波  杨世春  姬芬竹
作者单位:北京航空航天大学 交通科学与工程学院,北京 100191
摘    要:针对高空小型飞机的动力要求,对某型航空活塞发动机的进排气系统均匀性进行了分析,建立了某型航空活塞发动机的仿真模型,分析了进排气管路结构参数对发动机性能的影响.以进气质量流量不均匀度和进气压力波动效应为评价指标,对发动机的进排气系统结构参数进行了优化.通过改变进排气歧管和总管的长度,把不均匀度降低到5%以内,最大降幅为38%,并且提高了发动机的扭矩和功率,最大提高幅度为5%. 

关 键 词:航空活塞发动机    进排气系统    进气质量流量    不均匀度    压力波动    涡轮增压
收稿时间:2012/12/28 0:00:00

Optimization analysis of a aircraft piston engine intake and exhaust system
XU Bin,LIU Bo,YANG Shi-chun and JI Fen-zhu.Optimization analysis of a aircraft piston engine intake and exhaust system[J].Journal of Aerospace Power,2014,29(3):624-630.
Authors:XU Bin  LIU Bo  YANG Shi-chun and JI Fen-zhu
Institution:School of Transportation Science and Engineering, Beijing University of Aeronautics and Astronautics, Beijing 100191, China
Abstract:To meet the power requirement of small high altitude aircraft, the intake and exhaust system flow uniform of a aircraft piston engine was analyzed. Simulation model of the aircraft piston engine was established, and the effects of intake and exhaust pipe structural parameters on engine performance were analyzed. The intake mass flow unevenness and pressure fluctuations were chosen as evaluating indicators to optimize the structural parameters of the engine's intake and exhaust system. By changing the length of intake manifold and duct, the unevenness is reduced to less than 5%, and the biggest decrease amplitude is 38%; the engine power and torque are improved by 5%.
Keywords:aircraft piston engines  intake and exhaust system  intake mass flow  unevenness  pressure fluctuation  turbocharging
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