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静子容腔泄漏对某压气机性能影响的数值研究
引用本文:陈美宁,谢伟亮,王红涛.静子容腔泄漏对某压气机性能影响的数值研究[J].航空动力学报,2014,29(11):2543-2549.
作者姓名:陈美宁  谢伟亮  王红涛
作者单位:中国航空工业集团公司 中航商用航空发动机有限责任公司, 上海 201108;中国航空工业集团公司 中航商用航空发动机有限责任公司, 上海 201108;中国航空工业集团公司 中航商用航空发动机有限责任公司, 上海 201108
摘    要:利用全三维数值模拟方法研究了压气机静子容腔泄漏流动对压气机性能以及流场的影响,研究表明静子容腔泄漏流动不仅导致压气机效率和压比降低,而且使得压气机提前失速,稳定裕度下降5.19%.详细流场分析显示静子容腔泄漏流动对上游叶片排流动影响较小,但对本级静子以及后面叶片排根部流场的影响明显,静子容腔泄漏流动还改变了压气机失速的原因:静子容腔泄漏流动导致第1级静子根部尾缘发生流动分离,使得第2级转子根部攻角过大,整个叶背发生流动分离,引起压气机提前失速.

关 键 词:压气机  静子  容腔  泄漏流动  稳定裕度
收稿时间:7/7/2013 12:00:00 AM

Numerical investigation of stator cavity leakage influence to a compressor performance
CHEN Mei-ning,XIE Wei-liang and WANG Hong-tao.Numerical investigation of stator cavity leakage influence to a compressor performance[J].Journal of Aerospace Power,2014,29(11):2543-2549.
Authors:CHEN Mei-ning  XIE Wei-liang and WANG Hong-tao
Institution:Aviation Industry Corporation of China Commercial Aircraft Engine Company Limited, Shanghai 201108, China;Aviation Industry Corporation of China Commercial Aircraft Engine Company Limited, Shanghai 201108, China;Aviation Industry Corporation of China Commercial Aircraft Engine Company Limited, Shanghai 201108, China
Abstract:Three-dimensional numerical simulations were carried out for a compressor to investigate the stator cavities' influence to the performance and flow field. Detailed analyses of the performance and flow field came to some conclusions: the cavity leakage flow led to decreases in the efficiency, pressure ratio and stall margin of the compressor. The compressor stall margin declines by 5.19% due to the cavity leakage flow. The cavity leakage flow mainly influences the root flow of the stator and rear blades, and changes the compressor stall mechanism. The cavity leakage flow causes flow separation near the hub of the first stator, as a result the second rotor incidence angle increase sharply; consequently the flow separates at the suction side of the second rotor, causing the compressor stall earlier than that without the cavity.
Keywords:compressor  stator  cavity  leakage flow  surge margin
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