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航空活塞发动机机体疲劳优化设计方法
引用本文:邹湘伏,邓宇,潘钟键.航空活塞发动机机体疲劳优化设计方法[J].航空工程进展,2020,11(4):603-608.
作者姓名:邹湘伏  邓宇  潘钟键
作者单位:湖南山河科技股份有限公司 航空研究院,株洲 412000;山河智能装备股份有限公司 国家企业技术中心,长沙 410100,湖南山河科技股份有限公司 航空研究院,株洲 412000;山河智能装备股份有限公司 国家企业技术中心,长沙 410100,长沙学院 机电工程学院,长沙 410022;山河智能装备股份有限公司 国家企业技术中心,长沙 410100
基金项目:湖南省科技计划-长株潭国家自主创新示范区专项2018XK2204
摘    要:机体可靠性差是航空活塞发动机适航取证过程中的技术难题。以某型发动机下机体为研究对象,通 过模型仿真得到机体的瞬态载荷曲线并进行拟合,按实际安装对其进行约束,采用 Goodman方法进行高周疲 劳分析,计算机体疲劳安全系数;提出一种分离式主轴盖的设计方法,优化下机体结构,在相同载荷的条件进行 对比分析;采用威布尔数学模型对机体可靠性指标进行计算验证,并对优化后的机体进行耐久测试。结果表 明:下机体疲劳安全系数、整机寿命、可靠性大幅提升,该设计方法对提高类似结构可靠性有一定的借鉴意义。

关 键 词:机体  瞬态载荷  高周疲劳  分离式主轴盖  疲劳安全系数
收稿时间:2020/3/24 0:00:00
修稿时间:2020/4/28 0:00:00

Fatigue optimization design method for block of aero piston engine
Zou Xiangfu,Deng Yu and Pan Zhongjian.Fatigue optimization design method for block of aero piston engine[J].Advances in Aeronautical Science and Engineering,2020,11(4):603-608.
Authors:Zou Xiangfu  Deng Yu and Pan Zhongjian
Institution:Hunan Sunward Science and Technologies Co., Ltd,Hunan Sunward Science and Technologies Co., Ltd,Sunward Intelligent Equipment Co., Ltd
Abstract:Poor reliability of engine block is a technical problem in airworthiness certification of aviation piston engine. Taking the engine block of a certain type of engine as the research object, the transient load curve of the engine block is obtained and matched through the model, and it is restrained according to the actual installation. The Goodman method is used to analyze the high cycle fatigue of the engine block, the fatigue safety factor of block is obtained. A design method of separated main bearing cap is put forward to optimize the structure of the lower engine block, and the comparative analysis is carried out under the same load conditions. The analysis results show that the fatigue safety factor of the lower block and engine life are improved, and the reliability index is verified by Weibull mathematical model. The durability test of the optimized engine block shows that the reliability of the engine block is improved, which proves that the design method is feasible, and it can be used for reference to improve the reliability of similar structures.
Keywords:block  transient load  high cycle fatigue  separated  fatigue safety factor
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