首页 | 本学科首页   官方微博 | 高级检索  
     检索      

CK-1M无人机双发助推器脱落分析与研究
引用本文:施允涛.CK-1M无人机双发助推器脱落分析与研究[J].南京航空航天大学学报,1994(1).
作者姓名:施允涛
作者单位:南京航空航天大学无人机研究所
摘    要:本文分析研究了无人机取发助推器的脱落安全性,研究对象是CK-1M无人机。根据风洞投放试验结果,设计了一对截锥体、截锥窝自动分离接头,从而改变了脱落方式,并调整了发射参数,以减小分离速度。同时确保双发助推器的同步性和安装对称性,消除了侧滑的影响;又因加上助推器增重,降低了助推器的投放轨迹,实现了CM-1M双发助推器的安全投放。

关 键 词:无人机  助推器  同步,投放轨迹  分离速度

Analysis and Study of Dropping of Two Boosters of the CK-1M Pilotless Aircraft
Shi Yuntao.Analysis and Study of Dropping of Two Boosters of the CK-1M Pilotless Aircraft[J].Journal of Nanjing University of Aeronautics & Astronautics,1994(1).
Authors:Shi Yuntao
Abstract:The drop safety of the boosters of the CK-1M pilotless aircraft is studied in this paper. According to the result of the drop test in the wind tunnel, an automatic unlocking joint is designed for a pair of the truncated cone and the socket, then the way of dropping out is changed, so that the launching parameters are adjusted in order to reduce the separation velocity. At the same time, as the synchronism and mounting symmetry of two boosters are ensured, it will result in eliminating the sideslip effects, and the boosters weight are increased. All mentioned reasons result in reducing the throwing locus. Thus,the drop for two boosters of the CK-1M pilotless aircraft will be accomplished safely.
Keywords:pilotless aircraft I booster  synchronism  throwing locus  separation velocity  
本文献已被 CNKI 等数据库收录!
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号