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H2O污染对煤油燃料超燃冲压发动机燃烧室性能影响的数值模拟
引用本文:邢建文,肖保国.H2O污染对煤油燃料超燃冲压发动机燃烧室性能影响的数值模拟[J].航空动力学报,2012,27(11):2408-2413.
作者姓名:邢建文  肖保国
作者单位:1. 南京航空航天大学能源与动力学院,南京210016 中国空气动力研究与发展中心超高速空气动力研究所高超声速冲压发动机技术重点实验室,四川绵阳621000
2. 中国空气动力研究与发展中心超高速空气动力研究所高超声速冲压发动机技术重点实验室,四川绵阳,621000
摘    要:在超声速燃烧设备上进行了带凹槽的直连式双模态煤油燃料超燃冲压发动机污染与纯空气来流的对比试验.为了研究来流污染对超燃冲压发动机试验性能的影响,在相同的试验气体参数(马赫数为2,总温约为828K和总压约为800kPa)下,对带凹槽煤油燃料燃烧室进行了一系列对比燃烧试验.采用AHL3D软件对3个试验条件的燃烧室反应流场进行了数值模拟.计算和试验得到的压强分布比较接近且趋势一致.通过数值模拟获得反应流场的细节,探究污染影响的机理.

关 键 词:超燃冲压发动机  燃烧室  污染效应  性能  燃烧效率
收稿时间:2011/10/31 0:00:00

Numerical simulation of H2O vitiation effects on kerosene-fueled scramjet combustor performance
XING Jian-wen and XIAO Bao-guo.Numerical simulation of H2O vitiation effects on kerosene-fueled scramjet combustor performance[J].Journal of Aerospace Power,2012,27(11):2408-2413.
Authors:XING Jian-wen and XIAO Bao-guo
Institution:College of Energy and Power Engineering, Nanjing University of Aeronautics and Astronautics, Nanjing 210016, China;Science and Technology on Scramjet Laboratory, Hypervelocity Aerodynamics Institute of China Aerodynamics Research and Development Center, Mianyang Sichuan 621000, China;Science and Technology on Scramjet Laboratory, Hypervelocity Aerodynamics Institute of China Aerodynamics Research and Development Center, Mianyang Sichuan 621000, China
Abstract:Experiments on the direct-connect dual-mode Kerosene-fueled scramjet engine with two cavities were conducted in the supersonic combustion facility to compare the combustor performance under clean air and air vitiated with H2O conditions.The primary objective was to understand the complicated issues with regard to the effects of air-stream vitiation on scramjet test performance.A set of comparative combustion tests were conducted with the same test gas parameters of nominal Mach number 2,total temperature of about 828K and total pressure of about 800kPa.The simulations of reacting flowfield in the combustor under the same experimental conditions were conducted using flow solver AHL3D.The calculation results were close to experimental data.The final objective was to provide insight into the detail of combustion flow which was not resolved by the available instruments.
Keywords:scramjet  combustor  vitiation effect  performance  combustion efficiency
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