首页 | 本学科首页   官方微博 | 高级检索  
     检索      

降低N_2O_4-UDMH发动机热流强的添加剂
引用本文:潘世安.降低N_2O_4-UDMH发动机热流强的添加剂[J].航空学报,1980,1(2):62-66.
作者姓名:潘世安
摘    要: 本文介绍了添加剂甲基硅酮降低硝基氧化剂-偏二甲基肼(UDMH)发动机热流强的研究情况和试验结果。论述了降低热流强与提高液体火箭发动机性能之间的关系。叙述了添加剂——甲基硅酮的性质和用添加剂降低推力室热流强的机理。分析试验结果指出:添加剂甲基硅酮(SiOC2H6n的粘度在20℃下应低于13厘斯;UDMH中添加1重量%硅酮后,推进剂使用性质略有改善,推力室总热流下降约33%。

关 键 词:
收稿时间:1980-02-01;

AN APPROACH OF INCREASING LIQUID ROCKET ENGINE PERFORMANCE--STUDY ON HEAT FLUX REDUCTION IN N_2O_4-UDMH ENGINE
Pan Shian.AN APPROACH OF INCREASING LIQUID ROCKET ENGINE PERFORMANCE--STUDY ON HEAT FLUX REDUCTION IN N_2O_4-UDMH ENGINE[J].Acta Aeronautica et Astronautica Sinica,1980,1(2):62-66.
Authors:Pan Shian
Abstract:This paper presents the study and the testing results of reducing heat flux in nitro-group-oxidizer-unsymmetrical dimethylhydrazine engine with additive methyl silicone. The relationship between heat flux reduction and improvement of rocket engine is discussed. The properties of additive methyl silicone and the mechanism of heat flux reduction in the thrust chamber are described. Analysis of testing results shows that the viscosity of additive silicone (SiOC2H6)n should be less than 13 centistoke at 20℃; when 1wt% Si is added into UDMH, there is slight improvement in the operational property of pro-pellant;and the total heat flux of the thrust chamber has been reduced about 33% .
Keywords:
本文献已被 CNKI 等数据库收录!
点击此处可从《航空学报》浏览原始摘要信息
点击此处可从《航空学报》下载免费的PDF全文
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号