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轴流风扇/压气机气动性能试验若干问题探讨
引用本文:向宏辉,侯敏杰,葛宁,刘志刚,温珍荣.轴流风扇/压气机气动性能试验若干问题探讨[J].航空动力学报,2015,30(6):1423-1431.
作者姓名:向宏辉  侯敏杰  葛宁  刘志刚  温珍荣
作者单位:南京航空航天大学 能源与动力学院, 南京 210016;中国航空工业集团公司 中国燃气涡轮研究院, 四川 江油 621703,中国航空工业集团公司 中国燃气涡轮研究院, 四川 江油 621703,南京航空航天大学 能源与动力学院, 南京 210016,中国航空工业集团公司 中国燃气涡轮研究院, 四川 江油 621703,中国航空工业集团公司 中国燃气涡轮研究院, 四川 江油 621703
摘    要:为提高航空发动机风扇/压气机试验流程控制的合理性和试验结果评定的真实性,在梳理国内航空发动机压缩部件气动性能试验研究现状的基础上,总结提炼出若干重要技术问题,并通过理论分析和部分试验验证,对所涉及的技术问题进行了深入探讨.分析结果表明:风扇气动性能试验和压气机气动性能试验对试验设备排气能力的要求不同;相比升转速录取方式,降转速录取能够优化风扇/压气机的试验流程;可采取不同措施降低测量探针对风扇/压气机试验结果的固有影响;可调导叶/静叶安装角度定位与全行程调节精度是影响变几何多级压气机气动性能试验结果重复性的主要因素.

关 键 词:轴流风扇  轴流压气机  气动性能  试验流程  重复性
收稿时间:2014/8/25 0:00:00

Discussion on several problems of axial flow fan/compressor aerodynamic performance experiment
XIANG Hong-hui,HOU Min-jie,GE Ning,LIU Zhi-gang and WEN Zhen-rong.Discussion on several problems of axial flow fan/compressor aerodynamic performance experiment[J].Journal of Aerospace Power,2015,30(6):1423-1431.
Authors:XIANG Hong-hui  HOU Min-jie  GE Ning  LIU Zhi-gang and WEN Zhen-rong
Institution:College of Energy and Power Engineering, Nanjing University of Aeronautics and Astronautics, Nanjing 210016, China;China Gas Turbine Establishment, Aviation Industry Corporation of China, Jiangyou Sichuan 621703, China,China Gas Turbine Establishment, Aviation Industry Corporation of China, Jiangyou Sichuan 621703, China,College of Energy and Power Engineering, Nanjing University of Aeronautics and Astronautics, Nanjing 210016, China,China Gas Turbine Establishment, Aviation Industry Corporation of China, Jiangyou Sichuan 621703, China and China Gas Turbine Establishment, Aviation Industry Corporation of China, Jiangyou Sichuan 621703, China
Abstract:In order to improve the rationality of experimental process control and the authenticity of experimental results assessment of aero-engine fan/compressor, several important technology problems were summarized by analyzing the aerodynamic performance experimental research situation of the domestic aero-engine compression components. Through theoretical analysis and partial experimental validation, these technology problems were discussed in depth. The analysis results show that the requirements of experimental facility exhaust system ability are different for fan aerodynamic performance experiment and compressor aerodynamic performance experiment; compared with the method of rising rotating speed collection, decreasing rotating speed collection can optimize the fan/compressor experimental process; the inherent effects of measuring probes on fan/compressor experimental results can be reduced through different methods; the stagger angle positioning and full stroke adjustment accuracy of the adjustable guide vane/stator vane are the main influential factors to the repeatability of aerodynamic performance experimental results of variable geometry multistage compressors.
Keywords:axial flow fan  axial flow compressor  aerodynamic performance  experimental process  repeatability
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