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双级对转压气机全工况优化设计
引用本文:张鹏,刘波,曹志远,史磊.双级对转压气机全工况优化设计[J].航空动力学报,2014,29(10):2434-2442.
作者姓名:张鹏  刘波  曹志远  史磊
作者单位:西北工业大学 动力与能源学院, 西安 710072;西北工业大学 动力与能源学院, 西安 710072;西北工业大学 动力与能源学院, 西安 710072;西北工业大学 动力与能源学院, 西安 710072
基金项目:国家自然科学基金(51236006)
摘    要:为全面提升对转压气机气动性能,以某双级对转压气机为研究对象,基于人工神经网络与遗传算法,针对转子2叶片在整机环境下进行全工况优化设计,并对优化前后几何形状、总体性能及流场结构进行了对比分析.结果表明:优化后对转压气机全工况范围内等熵效率及压比均得到提升,同时流量范围有所增大.在设计点整机等熵效率提高0.3%,近失速点整机等熵效率提高1.5%,喘振裕度上升了6.37%,稳定工作范围得到显著扩大.优化后转子1全工况范围内等熵效率和压比特性变化不大,而转子2全工况范围内等熵效率和压比均有较大提高,其中在设计点转子2等熵效率上升1%,近失速点转子2等熵效率上升2.5%;在近失速点,优化后转子1、转子2、出口导叶(OGV)尖部流场显著改善.

关 键 词:对转  压气机  全工况  优化设计  等熵效率
收稿时间:2013/6/28 0:00:00

Optimization design of a two-stage counter-rotating compressor under overall working conditions
ZHANG Peng,LIU Bo,CAO Zhi-yuan and SHI Lei.Optimization design of a two-stage counter-rotating compressor under overall working conditions[J].Journal of Aerospace Power,2014,29(10):2434-2442.
Authors:ZHANG Peng  LIU Bo  CAO Zhi-yuan and SHI Lei
Institution:School of Power and Energy, Northwestern Polytechnical University, Xi'an 710072, China;School of Power and Energy, Northwestern Polytechnical University, Xi'an 710072, China;School of Power and Energy, Northwestern Polytechnical University, Xi'an 710072, China;School of Power and Energy, Northwestern Polytechnical University, Xi'an 710072, China
Abstract:In order to improve aerodynamic performance of the counter-rotating compressor in an all-round way, overall working conditions optimization design was carried out on the Rotor 2 of a two-stage counter-rotating compressor in multistage environment based on artificial neural network and genetic algorithm. The changes of geometry, overall performance and flow field were compared and analyzed. Results show that: after the optimization, the overall isentropic efficiency and pressure ratio of the counter-rotating compressor are both improved, meanwhile the range of mass flow is widened. The isentropic efficiency of the counter-rotating compressor increases by 0.3% on the design point, increases by 1.5% near the stall point, and the surge margin increases by 6.37%. After the optimization, the overall isentropic efficiency and pressure ratio of the Rotor 1 are almost unchanged, but those of Rotor 2 are raised much. The isentropic efficiency of Rotor 2 improves by 1% on the design point, and the isentropic efficiency is improved by 2.5% near the stall point. Also, the flow fields of Rotor 1, Rotor 2 and outlet guide vane (OGV) at the tip are improved remarkably near the stall point.
Keywords:counter-rotating  compressor  overall working conditions  optimization design  isentropic efficiency
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