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面向航空发动机减重的铝合金管强化机理研究
引用本文:屈力刚,荆麒瑀,李铭,杨英铎.面向航空发动机减重的铝合金管强化机理研究[J].航空制造技术,2021(5):14-23.
作者姓名:屈力刚  荆麒瑀  李铭  杨英铎
作者单位:沈阳航空航天大学机电工程学院
基金项目:校引进人才科研启动基金项目(18YB58)。
摘    要:为助推新一代大型航空发动机推重比的有效提升,开展面向航空发动机减重需求的高强度铝合金管件自增强机理研究。采用有效强化的高强度铝合金管件大规模替换航空发动机低温段不锈钢高压管件,是实现航空发动机减重的可行方法。通过研究高强度铝合金管件自增强工艺的强化机理,建立基于三剪统一强度准则,同时考虑包辛格效应、应变时效以及应变硬化的高压自增强工艺参数数学模型,并结合双线性随动强化模型,分析管路构件在强化过程中的弹塑性行为与残余应力分布演化规律,研究确定强化工艺参数。基于ANSYS,在额定工况下对强化后的铝合金管件和不锈钢管件的疲劳强度进行仿真分析,最后采用脉冲疲劳试验进行验证,证明自增强铝合金管件替换现役不锈钢管件具有较好的可行性。

关 键 词:航空发动机  减重  自增强  工艺参数优化  疲劳强度

Research on Strengthening Mechanism of Aluminum Alloy Pipe for Aero-Engine Weight-Reduction
QU Ligang,JING Qiyu,LI Ming,YANG Yingduo.Research on Strengthening Mechanism of Aluminum Alloy Pipe for Aero-Engine Weight-Reduction[J].Aeronautical Manufacturing Technology,2021(5):14-23.
Authors:QU Ligang  JING Qiyu  LI Ming  YANG Yingduo
Institution:(College of Mechanical and Electrical Engineering,Shenyang Aerospace University,Shenyang 110136,China)
Abstract:In order to promote the effective improvement of thrust-to-weight ratio of new generation of large aeroengines,the research on autofrettage mechanism of high-strength aluminum alloy pipe fittings for aero-engine weightreduction requirements was carried out.It is a feasible way to reduce the weight of aero-engines that using effectively strengthened high-strength aluminum alloy pipe fittings to replace stainless steel high-pressure pipe fittings in the low temperature section of aero-engine on a large scale.To obtain the mathematical model of the high-pressure autofrettage process of aviation pipeline,the strengthening mechanism of high-pressure pipeline autofrettage process was researched and Bauschinger effect,strain aging and strain hardening based on the triple shear unified failure criterion were considered.The bilinear kinematic hardening model was used to analyze the elasto-plastic behavior of the pipeline during the hardening process and the evolution of the residual stress distribution.Based on ANSYS,the fatigue strength of reinforced aluminum alloy pipe and stainless steel fittings were simulated and analyzed under rated conditions.Finally,pulse fatigue experiments were done to verify that it is feasible to replace existing stainless steel fittings with strengthened aluminum alloy pipe fittings.
Keywords:Aero-engine  Weight-reduction  Autofrettage  Process parameter optimization  Fatigue strength
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