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减速板对水平尾翼的干扰研究
引用本文:齐孟卜,陈明岩.减速板对水平尾翼的干扰研究[J].南京航空航天大学学报,1997,29(3):317-320.
作者姓名:齐孟卜  陈明岩
作者单位:南京航空航天大学空气动力学系
摘    要:在NH-2风洞中对某机放减速板产生较大抬头力矩的机理进行了研究,通过减速板分离涡场的测量和测力试验表明,抬头力矩主要是由减速板分离涡在平尾处产生在的诱导下洗角所致,诱导下洗角涡机身轴线向后逐渐减小,减速板前移可以消除抬头力矩。保持原减速板位置不动时,减速板开孔减小涡强度可以减小抬头力矩,选择适当的减速板开孔率和开孔位置能使抬头力矩减小到可以接受的程度并且保持具有足够的阻力。

关 键 词:减阻  分离流动  减速板  分离涡场  尾翼  水平尾翼

On the Research of Interactions of Drag Plate the Tail
Qi Mengbu,Chen Mingyan.On the Research of Interactions of Drag Plate the Tail[J].Journal of Nanjing University of Aeronautics & Astronautics,1997,29(3):317-320.
Authors:Qi Mengbu  Chen Mingyan
Abstract:The principle of the increase of the nose up pitching moment by opening the drag plate for an airplane has been studied in NH 2 wind tunnel. The measurements of the separated vortex field and forces for drag plate show that the nose up pitching moment is produced due to the large induced downwash angle from the separated vortices of drag plate at the tail. The induced downwash angle is reduced asymptotically along the axis of fuselage. The nose up pitching can be eliminated by moving drag plate forword to suitable location. If the location of drag plate is kept still, making use of the porous drag plate can reduce the vorticity and the nose up pitching moment. The nose up pitching moment can be reduced to acceptable level and enough drag can be kept by the selection of suitable porosity and location of drag plate.
Keywords:drag reduction  separated flow  drag plate  separated vortex field  porosity of drag plate  downwash angle  nose  up pitching moment
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